A weekend spent mostly lying upside down where the driver's seat should be with my head under the dashboard has resulted in all the wiring and plumbing under there being completed. It has also resulted in the somewhat unusual phenomenon of footprints on the roll cage!
Both fire extinguisher and battery are now fully fitted and I've tested all of the wiring that I can at this stage. The good news is that it all works! There were a few minor things wrong but they were soon sorted out. Specifically;
The headlight flash didn't work due to two terminals on the switch being the wrong way round. Easily resolved though took some head scratching to figure it out. Now I know why I spent so long drawing up that circuit diagram.
The indicator relay was suffering the same problem (reversed connections).
The oil pressure warning light had a loose bulb.
I didn't think that was at all bad for the first test of a completely custom built wiring loom. There are a few things I can't test as I haven't fitted them yet but still a nice result so far.
Here are a couple of pictures of the new dash in situ.
The fuel pumps and filter have been refitted in the boot ready for the tank to be plumbed in. I decided to make a better mounting for the tank than the odd bits of bracketry I had before so that's on hold until I can get hold of some aluminium box and angle to do some fabrication work.
This weekend I started by fitting the front lighting to the bonnet and quarter valences. The sidelight/indicator units fitted easily and so did the left hand headlamp but when I fitted the right hand headlamp it was obviously sitting at an angle and the cowl wouldn't fit over it either. After a lot of measuring I re-drilled the mountings so it would sit straight and also moved it over about 2mm. Such are the joys of working with a glass fibre bonnet.
After that the cowl still didn't fit and there followed a lot of fitting, dismantling, measuring, refitting, fabrication of spacers, dismantling again and so on. After a disproportionate amount of effort though it all eventually went together properly and everything lines up so it actually looks quite good.
I only stripped one thread in each of the cast alloy cowls too. They really are a poor design.
So that actually completed all the main work I had planned to do before the end of this month. Today however, with assistance from my dad we assembled the engine and gearbox and lifted it into the car.
I didn't really know whether it would fit as the new gearbox has never actually been in the car yet so I didn't know what problems we might encounter.
In the end the gearbox went in easily. There was a problem however and it certainly wasn't one I had anticipated...
Either my engine has shrunk whilst it's been sitting around the garage or there's something wrong with the mounting points onto the suspension turrets! One engine mount fits easily but the other is an inch short...
Here are some close-up photos of the problem.
After I took these pictures I noticed that the engine was also not sitting straight in the car. Unbolting the right hand mounting and bolting in the left hand one allowed the engine to sit vertical and nicely central in the engine bay and also central to the hole in the bulkhead but of course the one inch gap is now on the other side.
That leads me to believe that the problem might be somewhere around the right hand mounting but I can't see anything that's not where it should be. I've also done some measuring and as far as I can tell the suspension turrets are where they should be with the top wishbone mounting bolts equally spaced either side of the centre line.
We tried two different sets of engine mounts. One brand new and the
other being the set that were on the engine previously. The back of the
gearbox isn't fastened to anything and is free to move around so that
can't be pulling anything out of line.
As far as I know
there's only one type of suspension turret but I may be wrong there. Is
it possible the turret from a different car has got in there during the
rebuild? If you have any ideas, please feel free to leave comments
below. Right now I'm out of ideas.
We both stared at this problem for quite a while and in the end we both gave up. I made a temporary bracket to hold the engine in position so that we could at least release it from the engine crane. I also started work on making a mounting bracket for the back of the new gearbox.
At least with the engine (roughly) in position I can get on with taking the measurements for the remainder of the wiring loom and I can also look at working out how things like the gearbox speed sender are going to fit. The gearbox seems quite close to the chassis at that point.
So several things sorted out but a new problem to deal with. Odd how these things come from the most unexpected directions sometimes.
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